So yesterday I noticed that during rapid roll movements the spherical rod end were moving on the bolt I used to hold them. There was .050 difference in the bolt diameter and the hole in the rod end. Tightening them helped a bit but wasn't the solution. I went to town to look for some cheap ball joints with a stud but all the cheap ones had the same runout. So I decided to give something a try and it worked like a charm. I turned down a steel rod to .080 oversized and pressed it into the hole of the rod end. The force of the pin expanded the steel ball to a snug fit with the brass sleeve, no measurable slack. Only took me three tries .010 oversized bent the pin before I could force it in and .050 was a nice fit but didn't effect the total runout. Saved me a few buck and was a good exercise in turning to a precise diameter.
Shawn
Shawn
Shawn, proud to be a member of MetalworkingFun Forum since Nov 2013.